This paper describes the effects of coolant-to-mainstream density ratio and specific heat capacity flux ratio (the product of blowing ratio and specific heat capacity ratio) on the overall cooling effectiveness of high pressure (HP) turbine vanes. Experimental measurements have been conducted at correct engine-matched conditions of Mach number, Reynolds number, turbulence intensity, and coolant-to-mainstream momentum flux ratio. Vanes tested were fully cooled production parts from an engine currently in service. A foreign gas mixture of SF6 and Ar was selected for injection as coolant in the facility so that density and blowing ratios were also matched to the engine situation. The isentropic exponent of the foreign gas mixture coincides with that of air. Full-coverage surface maps of overall cooling effectiveness were acquired by an infrared (IR) thermography technique at a range of mainstream-to-coolant temperature ratios. Measurements were subsequently scaled to engine conditions by employing a new theory based on the principle of superposition and a recovery and redistribution temperature demonstrated in previous papers. It is shown that the two aerodynamically matched situations of air- and foreign-gas-cooled experiments give virtually the same effectiveness trends and patterns. Actual levels differ, however, on account of specific heat capacity flux ratio differences. The effect is described and quantified by a one-dimensional analytical model of the vane wall. Differences in Biot number with respect to engine conditions are discussed as they also influence the scaling of turbine metal temperatures.
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November 2017
Research-Article
Effects of Coolant Density, Specific Heat Capacity, and Biot Number on Turbine Vane Cooling Effectiveness
S. Luque,
S. Luque
Department of Engineering Science,
University of Oxford,
Parks Road,
Oxford OX1 3PJ, UK
e-mail: salvador.luque@imdea.org
University of Oxford,
Parks Road,
Oxford OX1 3PJ, UK
e-mail: salvador.luque@imdea.org
Search for other works by this author on:
T. V. Jones,
T. V. Jones
Department of Engineering Science,
University of Oxford,
Parks Road,
Oxford OX1 3PJ, UK
University of Oxford,
Parks Road,
Oxford OX1 3PJ, UK
Search for other works by this author on:
T. Povey
T. Povey
Department of Engineering Science,
University of Oxford,
Parks Road,
Oxford OX1 3PJ, UK
University of Oxford,
Parks Road,
Oxford OX1 3PJ, UK
Search for other works by this author on:
S. Luque
Department of Engineering Science,
University of Oxford,
Parks Road,
Oxford OX1 3PJ, UK
e-mail: salvador.luque@imdea.org
University of Oxford,
Parks Road,
Oxford OX1 3PJ, UK
e-mail: salvador.luque@imdea.org
T. V. Jones
Department of Engineering Science,
University of Oxford,
Parks Road,
Oxford OX1 3PJ, UK
University of Oxford,
Parks Road,
Oxford OX1 3PJ, UK
T. Povey
Department of Engineering Science,
University of Oxford,
Parks Road,
Oxford OX1 3PJ, UK
University of Oxford,
Parks Road,
Oxford OX1 3PJ, UK
1Present address: Unit of High Temperature Processes, IMDEA Energy Institute, Avenida Ramón de la Sagra, 3, Móstoles 28935, Spain.
2Corresponding author.
Manuscript received January 20, 2017; final manuscript received May 10, 2017; published online July 19, 2017. Assoc. Editor: Ardeshir (Ardy) Riahi.
J. Turbomach. Nov 2017, 139(11): 111005 (11 pages)
Published Online: July 19, 2017
Article history
Received:
January 20, 2017
Revised:
May 10, 2017
Citation
Luque, S., Jones, T. V., and Povey, T. (July 19, 2017). "Effects of Coolant Density, Specific Heat Capacity, and Biot Number on Turbine Vane Cooling Effectiveness." ASME. J. Turbomach. November 2017; 139(11): 111005. https://doi.org/10.1115/1.4037029
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